Abstract:
Conversion of animal waste to biogas through anaerobic digestion processes can provide added value to manure as an energy resource and reduce environmental problems associated with animal wastes. An anaerobic digester located at the Kirk Carrell Dairy in Johnson County near Godley, Texas, has been renovated as a demonstration of current anaerobic digestion technology for treatment of animal waste and recovery of energy. Economic analysis indicates that energy credits alone are not enough to offset the cost of investing in a biogas production facility. Annual operating costs were estimated to be $21,400 with energy credits of $17,500 for electricity produced and used on-site. Credits for reduction of odors, insect pests and other environmental problems have not been included in the analysis.
Introduction
With the increasing size and regional concentrations of confined animal feeding operations (CAFOs), there is growing public concern over degradation of environmental quality caused by CAFO-generated wastes. In response to this, regulatory agencies are looking more closely at animal waste management practices and revising regulations to reduce environmental impact. CAFOs in Texas produce over 5 million tons (dry) of animal waste annually (Sweeten, 1994). Handling these wastes in compliance with stricter environmental regulations can have a significant economic impact on CAFOs. As a result, CAFO operators are beginning to consider waste management practices that convert wastes into higher value products. One approach to increasing the value of waste is to use it as an energy resource.
The amount of waste produced varies with the type of animal, but generally ranges from 60 to 85 kg (wet basis) per 1,000 kg live animal mass per day in intensive production systems. The energy potential of these wastes is given by the volatile solids (organic matter) content which ranges from 10 to 18% of the total wet waste or 75 to 85% of the dry weight (ASAE, 1997). The energy potential of the manure produced in Texas ranges from 12×1012 to 25×1012 Btu annually depending on the method used for conversion (Parker et al., 1997). This annual amount is equivalent to 12 to 25 billion cubic feet of natural gas.
Either biological or thermochemical conversion methods can be used to obtain energy from animal wastes. Anaerobic digestion, a biological conversion process, has a number of advantages for waste conversion. Fresh wastes have high moisture content (about 80%), making them unsuitable for most thermochemical processes, and their varied composition and high content of lignocellulosic material makes them unattractive for fermentation to ethanol or other products. Another advantage is that operators of CAFOs frequently are familiar with this type of process since anaerobic lagoons are an essential component of most current liquid waste treatment systems. Anaerobic digestion also has some advantages from a waste treatment standpoint. Microbial action in the lagoon substantially reduces chemical and biological oxygen demands (COD and BOD, respectively), total solids (TS), volatile solids (VS), nitrate nitrogen, and organic nitrogen in the waste stream. Coliform bacteria, other pathogens, insect eggs and internal parasites also are destroyed or reduced to acceptable levels by anaerobic treatment.
In 1995, the Texas Agricultural Experiment Station began a project to renovate an anaerobic
digester located at the Kirk Carrell Dairy in Johnson County near Godley, Texas, as a demonstration
of current anaerobic digestion technology for treatment of animal waste and recovery of energy. The
digester originally was installed in 1984 to generate enough electricity to operate the dairy and have
surplus to sell to the local utility. Unfortunately, biogas production from the digester did not meet
expectations and operation was abandoned after about a year. The challenge for the renovation
project has been to identify shortcomings in the original design and develop modifications to
overcome these. In addition to providing power for the dairy, the renovated system will reduce the
potential for water pollution.
Background
Anaerobic digestion is a microbial process that occurs in the absence of oxygen. In the
process, a community of microbial species breaks down both complex and simple organic materials,
ultimately producing methane and carbon dioxide. Anaerobic digestion can occur over a wide range
of environmental conditions, although narrower ranges are needed for optimum operation (Table 1).
Temperature has a significant effect on digestion rate with most processes occurring at temperatures
in the mesophilic temperature range of 75-100F, but anaerobic digestion also can be carried out at
thermophilic temperatures (125-140F). Although methane production has been observed at
temperatures as low as 50F, the rate is quite slow which is why anaerobic lagoons generally do not
function in the winter.
Table 1. Operating conditions for anaerobic digestion processes.
| Operating Parameter | Typical Value |
| Temperature
Mesophilic Thermophilic |
95F 130F |
| pH | 7 - 8 |
| Alkalinity | 2500 mg/L minimum |
| Retention time | 10 - 30 days |
| Loading rate | 0.15 - 0.35 lb VS/ft3/d |
| Biogas yield | 3 - 8 ft3/lb VS |
| Methane content | 60 - 70% |
Anaerobic digestion is slower than aerobic waste treatment processes, typically requiring
retention times of 10-30 days for mesophilic digestion. Thermophilic digestion is more rapid, but
requires more energy to heat the digester. Loading rates (rates at which organic material is fed to the
digester) are based on volatile solids content of the feed and generally are in the range of 0.15-0.35
lb VS/ft3d for mesophilic processes. Biogas yields are in the range of 3-8 SCF/lb VS, and methane
content of the biogas usually is 60-70% with the balance mostly CO2. Trace amounts of hydrogen
sulfide (H2S), which is both toxic and corrosive, also are produced.
Energy Production
The Carrell Dairy currently milks about 400 cows, and the amount of biogas produced should be enough to supply the energy needs of the dairy. Several factors may have contributed to poor performance of the original installation, the most significant being a low feed rate to the digester. We do not have original design calculations, but it appears that the amount of manure that would be available to feed to the digester was substantially overestimated. To exacerbate this problem, the number of cows being milked was reduced after the system was designed.
The dairy originally housed all cows on a dry lot, with feed to the digester consisting of only
the manure and flush water from the milking parlor area. As part of the renovation, a freestall barn
housing 180 cows has been added which will allow collection of all the manure from the animals
housed there. About 220 more cows are housed on the dry lot, and we expect that about 25% of
their manure will be collected to feed the digester. Total feed to the digester should be about 3300
lb VS daily. Laboratory studies of digestion of dairy waste have given biogas yields of about 6.4
SCF/lb VS, so the digester should produce about 20,000 SCF/d of biogas. The energy content of
biogas is about 600 Btu/ft3, and assuming a conversion efficiency in the engine/generator system of
25%, we should be able to generate an average of 37 kW. Records of electrical usage at the Carrell
Dairy over a one-year period indicate an average demand of about 25 kW in winter and 35 kW in
summer with spikes up to 50 kW when motors are started. Therefore, we should be able to produce
enough biogas to provide all the power required for the dairy.
System Description
The original digester system consisted of a plug flow digester tank, a rubber/fabric gas bag covering the tank, a 100 hp engine driving a 65 kW generator, and a hot water circulating system to maintain the digester at an operating temperature of about 95F using waste heat from the engine. A metal building was constructed over the tank to protect the gas bag, and a smaller metal building housed the engine/generator system and electrical gear. When the renovation project started, we found the gas bag was rotted, and the building housing the tank was severely corroded. We decided to replace the building and gas bag with a lightweight reinforced concrete plank cover over a hypalon membrane to contain the gas, eliminating the need for a building. Although replacing the gas bag would have been less expensive, the bag would have had a shorter life span and would not have allowed placement of access ports along the length of the digester to be used for monitoring instrumentation, sampling, or installation of additional equipment.
The digester tank, which has not been modified, is a rectangular concrete tank 18 ft wide by 104 ft long with a V-shaped bottom. The tank is 8 ft deep at the sides and 12 ft 10 in. deep at the centerline. The outlet overflow is 30 in. below the top of the tank giving a liquid volume of 110,000 gal. A 4 ft opening was left at each end of the tank when the new cover was installed to provide access. The hypalon liner is a continuous sheet extending below the liquid level on each side and folded over the edge of the tank to be held by the concrete planks. The liner also extends below the liquid level at each end and is held in place by 3/4 in. thick fiberglass panels. Although a safety relief valve is installed on the gas line, the end curtains provide additional protection from excess pressure in the tank.
The original heat exchanger, which maintained the digester temperature at 95F, consisted of 4 pipe loops supported in a vertical plane down the center of the tank. The pipes were found to be severely corroded when the digester was cleaned out at the beginning of the project and so were removed. Since the primary heat load is to raise the feed temperature to 95F, the new heat exchanger was installed in the inlet end of the tank. New plumbing has been installed for the temperature control loop, but the general design is similar to the original. The antifreeze solution which circulates through the heat exchange pipes in the digester is heated by waste heat from the engine to a temperature of 140-150F. If the water circulating to the digester is hotter than 150F, some of the microbes may die causing a decline in gas production.
Although there is some mixing in the digester due to gas production and convection currents caused by the heat exchanger, there is not enough to keep solid particles in the feed from settling or forming a crust on the top of the liquid. To increase the mixing in the inlet end of the digester, biogas is recirculated to gas spargers placed under the heat exchange units. The recirculated gas along with natural convection currents generated by the heat exchanger should keep solids suspended, allowing them to move toward the outlet as feed is added. We have not provided mixing downstream of the inlet section, but gas spargers can be added through access ports at other locations if needed.
The original mechanical system included a 100 hp oil-field engine coupled to a 65 kW generator. The estimated cost for overhauling the engine was about $20,000, whereas a new engine/generator set based on an automotive engine cost less than $10,000. While the service life for an automotive engine is not as long as for the oil-field engine and it is somewhat less energy efficient, it is easier to obtain parts for it and perform routine maintenance. The system which was selected is similar to systems designed for powering irrigation pumps in remote locations. The new system consists of a 454 cubic inch displacement industrial engine, which can develop 150 hp at 1800 rpm, coupled to a synchronous generator rated for 60 kW in continuous duty. This generator is larger than needed for the demand created by the dairy; however, a smaller generator that would more closely match the demand would have required the same size engine since the next size smaller engine would be too small. While the larger generator may not be quite as efficient, it provides additional capacity that could be used for expansion of the dairy or to provide power for an adjacent dairy if enough biogas is produced.
The generator originally was connected in parallel with the utility grid so that excess electricity could be sold; however, most of the equipment for controlling the connection was not salvageable. Therefore, it was decided to connect the generator as a stand-alone system and flare any excess biogas produced. The utility grid is connected as a back-up for periods when the generator is down.
Hydrogen sulfide is a contaminant present in biogas at a concentration of around 1000 ppm. The original system did not have any provisions to remove the H2S from the biogas, which is not a problem as long as a rigorous engine maintenance schedule is followed. To reduce potential problems from H2S, a scrubber designed to remove H2S and other contaminants from natural gas has been installed in the gas fuel line for the engine.
Manure is scraped and flushed from the freestall barn and other paved areas into a collection pit. The bottom of the pit is sloped to drain flushed manure into a sump. A new manure slurry pump has been installed along with a recirculation line to flush the bottom of the collection pit. The original pump will be used as a back-up. In addition, a mechanical mixer has been added to the sump to keep the manure solids suspended in the slurry.
One goal of the project is to obtain operating characteristics of the digester over a period of
several years. To accomplish this we have included more monitoring instrumentation than normally
would be used for a biogas process. We will record temperatures, pressures and flow rates of the
gas going to both the engine and flare, temperatures at several locations in the digester, temperatures
of the water going to and returning from the digester heat exchanger, the flow rate of manure slurry
to the digester, and the power output of the generator. In addition, we will collect liquid and gas
samples from the digester on a weekly basis to determine compositions of these streams. As much
as possible, data collection is being automated to obtain more complete information.
Economic Analysis
The investment cost for the renovated system is $127,700 (Table 2). This is based on actual
installation cost for everything except the tank. Since the existing tank was utilized, its construction
cost was estimated using construction cost estimation data (Saylor, 1997). A 15-yr life was assumed
for all equipment except the engine, for which a 5-yr life was assumed. The annual cost of the
investment was determined by amortizing the investment at 7.5% over the life of the investment.
Repair and maintenance costs were estimated as 5% of investment cost and the risk variable was
included as 3% of investment cost. Annual costs related to the investment are summarized in Table
2.
Table 2. Investment costs for Carrell Dairy anaerobic digester.
|
Item |
Life (yr) |
Investment |
Annual Cost1 |
Repairs &
Maintenance2 |
Risk3 |
| Tank
Cover Engine Generator Other Equipment Materials/Supplies Contractor |
15
15 5 15 15 15 15 |
$ 40,000
47,800 5,000 5,600 18,000 5,600 5,700 |
$ 4,215
5,037 1,150 590 1,897 590 601 |
$ 211
252 57 30 95 30 30 |
$ 126
151 34 18 57 18 18 |
| TOTAL | $ 127,700 | $ 14,080 | $ 705 | $ 422 |
1 Investment amortized at 7.5% for life of investment with no salvage value.
2 Estimated at 5% of annual investment cost.
3 Estimated at 3% of annual investment cost.
Table 3. Expected annual costs
| Item | Annual Cost |
| Investment
Repair & Maintenance Risk Variable (labor1, supplies2) |
$ 14,080
705 422 6,200 |
| TOTAL | $ 21,407 |
1 Labor estimated at 10 hr/wk at $10/hr.
2 Supplies estimated at $1,000.
Although this anaerobic digestion system probably could be operated with no additional labor required, we have included an increment of 10 hr/wk of labor at a cost of $10/hr for operating the system. Supplies needed for the operation have been estimated at $1,000 annually. The total expected annual costs are estimated to be $21,407 (Table 3).
The electricity generated using the digester biogas as fuel should be enough to make the dairy self-sufficient. Average electrical usage monitored at the dairy is 25 kW during the winter and 35 kW during the summer, with each rate occurring over about a six-month period. This gives a total annual electrical usage of 262,000 kWh. The cost of electricity for the dairy is 6.7¢/kWh, so the annual savings on electricity charges would be $17,500.
The expected annual costs are about $21,400 compared to an economic benefit of $17,500,
giving a net annual loss of about $4,000. These are first estimates and will be revised as we gain
operating experience with the digester. Also, this analysis does not include any credits for reduction
in odor, insect pests or other environmental concerns.
Environmental Benefits
Typically, animal waste management systems utilize anaerobic or facultative lagoons for treatment of liquid waste streams such as flush water and runoff and land application to dispose of solids. The solids may be stockpiled for a period of time before application can be made. Manure stockpiles and improperly operating lagoons can be sources of odors and insect pests which are nuisances for neighbors. Effluents from lagoons contain substantial nitrogen and phosphorus nutrient loads and must be applied to land for disposal. Effluents from well-designed and properly operated systems constitute a very low potential for nonpoint source pollution of water resources; however, unfavorable weather may significantly increase the pollution potential from these systems.
Enclosed anaerobic digestion systems for biogas production are not subject to pronounced influences of the weather making effluents from digesters more stable and uniform than effluents from anaerobic lagoons. Additionally, odors are controlled since all the gas is burned before being released into the atmosphere. Anaerobic digestion processes result in source strength reduction by converting incoming organic matter to methane, carbon dioxide and small amounts of microbial biomass; pathogens and weed seeds are destroyed; and odors are reduced. Total nitrogen, phosphorus and other minerals remain largely unchanged; therefore, effluent from a digester must be retained in a holding pond and used either as recycle flush water or for irrigation. The potential for nonpoint source pollution resulting from heavy rainfall is lessened since the influent to the holding pond will have undergone complete digestion.
Another environmental benefit from using biogas as an energy resource is that there is no net
production of greenhouse gases. The carbon dioxide released during biogas combustion originally
was organic plant material and so is just completing a cycle from atmosphere to plant to animal and
back to the atmosphere. Methane is a more severe greenhouse gas than carbon dioxide and capture
of biogas as a fuel prevents the release of methane into the atmosphere. Although less methane
probably is generated in land application of solids and anaerobic lagoon treatment of liquid wastes,
those processes still release a substantial amount of methane to the atmosphere. Capture of the
methane for use as a fuel would significantly reduce the net greenhouse gas production from CAFOs.
References
ASAE. 1997. Manure production and characteristics, ASAE D384.1 DEC93, ASAE Standards 1996, 44th Ed., ASAE The Society for Engineering in Agricultural, Food, and Biological Systems, St. Joseph, MI.
Saylor, Lee. 1997. Current Construction Costs, 34th Ed., Saylor Publications, Inc., Walnut Creek, CA.
Parker, D.B., B.W. Auvermann, B.A. Stewart and C.A. Robinson. 1997. Agricultural energy consumption, biomass generation, and livestock manure value in the southern high plains, Livestock Waste Streams: Energy and Environment, Texas Biomass Energy Opportunities Workshop Series, Amarillo, TX, August 4.
Sweeten, J.M., et al. 1994. Animal Waste Management Task Force Report, Agriculture Program, Texas A&M University System, College Station, September 27.